Once again it seems to be a while since I contributed here.
Since the last entry I met with some success & hit some more problems.
The new Idle Speed Control Valve didn't fix the fast idle,
but mounting it the other way up did, it seems I'd put the inlet / outlet holes
the wrong way round - in my defence, when it's mounted on the Focus manifold it
points sideways, will fit space & wire length wise either way round &
in contravention of good engineering practice, can be fitted pointing either
way, so I had nothing to go on when I designed the mounting plate - of course
the "Haynes-book-of-lies" was no help because I have a Focus part
& the Escort ISCV in the manual is completely different.
Mounting the ISCV the other way up cured the problem - but
inevitably led to another - namely that the valve now pointed upwards & the
bonnet wasn't going to shut. I re-designed the mounting plate with the airways
reversed & set the 3D printer going again, after a day & a half
something wasn't right - the print had a "fault line", it had started
printing 3mm to the left. DISASTER.
I re-started it, this time (after a day & a half) it
offset the print to the right!
I abandoned the 3D print file made with – in theory –
superior slicing software & re-made it using the software that came with
the printer, by now I was getting very short of black printing filament, but
two days later I had my finished part & it worked.
Another problem I was still to resolve last time was the
Intake Air Temperature sensor - it had been screwed into the intake duct - but
that wouldn't fit, I toyed with ideas like cutting a hole in the new duct - but
as it has a wire coil moulded in, that was going to get messy, I thought of drilling
the Mass Air Flow sensor body, but it's a carefully designed venturi that
relies on airspeed over the sensor, putting another obstruction in the way
would mess the reading RIGHT up. Then I was "struck by the bleedin'
obvious" & cut the hard plastic & brass mounting out of the soft
plastic duct, drilled a hole in the air filter centre cone (where it's solid)
& used polyurethane adhesive to stick the mounting there. It’s in the
airflow without disturbing it, it can't get sucked into the duct & it's
easily replaceable.
Good isn't it?
I assembled the radiator & made cooling pipes outof left-over bits of Escort, Focus & Fiesta, jury-rigging the cooling fan switch into the end of a cut-off branch pipe with a jubilee clip, filled the system with water & started the engine. It idled beautifully - but - the alternator light stayed on, the engine refused to rev above idle & when I turne the key off, it refused to be stopped. not the caughing & spluttering "running on" of a carb / distributor engine with a problem, but perfectly normal running.
I checked all the wiring to the alternator & even
replaced it - the light stayed resolutely on. I turned my attention to the
non-stopping & thought that as I’d put relays on both the fuel pump &
ECU feeds, maybe just the power coming up the line from the alt light bulb was
enough to hold the relays closed, I did some re-wiring - & it made no
difference, but it didn't always do it. After a lot of faffing I noticed the
warning light for the rear fogs was on with ignition & then found there was
5 volts in the earth line. Not the earths for the things on the centre console
- I'd fitted them & made sure of a proper earth, but the original car loom
was only earthing through the rear fog light bulbs. I fixed that - cutting another 10
yards of wiring out of the car in the process. I've come to the conclusion that
the original builder crocheted the car from electrical wiring, then put glass
fibre round the outside at the end.
Last weekend a chap from the SKCC bought a proper industrial
fault code reader round as neither of mine could connect to the ECU, his
couldn't either, but he applied some wizardry & over-rode some functions
& eventually computer found computer. There were no fault codes, which was kind of good
because it meant the wiring was all OK. We started the engine & I
demonstrated the strangeness with the revving ie with the air duct & Mass
Air Flow meter in place, it refused to rev, disconnect the MAF & it
spluttered & died, BUT - leave the MAF electrically connected & remove
the air duct (so there's no flow through the MAF) & the engine will rev.
The warmer it got the better it reved until it was very nearly normal - even with the MAF in line, the next
problem was that my jury-rigged temp switch mounting was too far from the flow
of hot water & when the engine got to 117 deg C (yes - A HUNDRED AND
SEVENTEEN) we pulled the plug & put a wire across the terminals, the fan
came on & the engine dropped to normal in about 30sec (it was BLOODY cold
out there).
What did I learn?
The ECU is wired correctly & all the sensors are sending
signals.
Even running big revs at 117C there was no oil smoke from the
sump breather so the engine seems to be in top condition.
When it runs well, it runs really well, so there's just a
fault to find somewhere.
So I have some jobs to be getting on with. Today I've taken
the alternator to the shop it came from (Burghfield Starters & Alternators - highly recommended) where the nice man confirmed it's working but told me
I'd had the alt light wire going to the wrong terminal (DOH! - I photographed
it before I took it off the old engine where it was working just fine) so the
alt light now goes out. I've removed the radiator & top hose as I need
to get a hose joiner with a proper mounting for the fan switch & improve some of the hose routes. I also fixed a
small leak or two & now need to wrap the rest of the engine bay wiring loom
nicely & make a couple of small electrical changes. I've started
tiddivating the dash, so it won't be too long before it's ready for the road,
but at the moment I have no work, so I won't be taxing the car until next month
at the earliest (sigh).